airknocker
Member
- Aug 21, 2002
- 52
- 0
Not to worry, the word is A/C 101,706&707 are leaving GYR to return to service, these were parked last April&May during BK. More of the same.
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Oh joy.....a band-aid for a sucking chest wound. That's the long term answer. Got anymore shortsighted gems CCY???airknocker said:Not to worry, the word is A/C 101,706&707 are leaving GYR to return to service, these were parked last April&May during BK. More of the same.
E-Trons,E-TRONS said:I understand the "ALABAMA SLAMMER" still has major flap issues.......and to think that this was once a perfectly good airplane.
The CCY fools will never learn Good thing they saved all that money so they can spend it to fix this pig !!!
Never under-estimate the power of stupid people in executive positions :down: :down:
I gotta laugh that Smartest Loser castigated Blueoceans for lack of fact-checking in the same post with a totally factless claim of "pilot error" as the cause of the 5-in-5 fatal USAir accidents of the 1990's. To be sure, pilot error is a factor in some of those accidents, but it's always easier to take the "mass media" easy sound-bite and blame the pilots without checking the history, or the facts.X-U said:I don't know where the seven is coming from, but the majority of the "5 in 5"Smartest Loser said:Wrong Wrong Wrong...blueoceans said:USAirways has performed its maintenance inhouse and had 7 mainline fatal incidents (plus 2 express ones).
http://www.airsafe.com/airline.htm
The accidents on Mainline were NEVER ...I repeat NEVER attributed to in-house maintenance…!!! They were pilot error.
So, that cleared up....Check your facts first before making yourself look bad.
SL
was not attributed to pilot error. 427 was found to be a design error (rudder servo),
the collision in LAX was attributed to an ATC error and the DC-9 in CLT was also an ATC error (lack of timely weather info). Both LGA accidents were found to be pilot error. The only other one I can think of is the BAE-146 shot down by a disgruntled, former agent.
If your info is correct that will be the 3rd maintenance ferry flight in less than a week. Or should we start calling them multiple test hops? That maintenance outsourcing looks like its really paying off! It looks like someone is due a promotion in CCY. :blink:wings396 said:I noticed tonight that A/C 700 had an RTF in IAH with a gear problem. Shows a ferry flight to PIT.......