allegheny1
Member
- Oct 1, 2002
- 84
- 0
Many Threads...Many opinions...This is what i see from dealing with the
day to day operation.
1. Crew shortage and flight cancellations.
This is not a new problem. It has been an ongoing situation over the
last 13 years...at least. The current shortages have been caused by a
diverse set of circumstances. Some of the problem has been caused by
sick calls...a senior pilot crew scheduler states you can t take 80
pilot sick calls a day and not have a problem. Additional problems
arise when reserve pilot p times..long vs short..are not managed in
a timely manor. Another part of the shortage has been created because
the mtc plan submitted to marketing for each schedule does not come
close to reality causing significant preplanned equipment subs which
depletes both aircraft and crew resources. Yet another part of the shortage
comes from improper planning. You can t schedule crews for a 13 hr 30 min
to 13 hr 59 min duty day operating through phl,lga,bos 3 or 4 times.
The theory that weather was an issue simply is not the case. The weather
only manifests and brings to light the real shortcomings.
2. Mtc planning
In my opinion one of the worst managed areas within the airline. As
stated above the mtc plan submitted to marketing rarely if ever matches
what is required. Heavy mtc requirements do not match nor do the needs
for what are called mtc windows...for the layperson that relates to late
originating aircraft.
We should all remember that summer..not to long ago...when 12 full lines
of 737-300/400 flying were cancelled because mtc got behind on c checks
and had fired the planner who warned senior management that this would
happen. What may not be known is that a team was working on cancelling
3 to 5 lines 757 flying in the days leading up to 9/11. The team was
informed that the f 100 would also be in this position shortly
thereafter. The tragedy on 9/11 effectively cured these problems.
Many of the middle and upper managers that helped to create the
problems are still in charge and similar situations are in the
process of rearing there ugly head. A lie,cheat, and steal attitude
has been prevelant for quite some time and continues unabated.
3. Business travel
Here is a microcosm of what probably are more significant issues. The
operating units were informed that the shuttle made a small profit in
April 2003 and a more significant profit in May 2003 while maintaining
2 spares and weekday standby crews. The marketing response in June 2003
was to split the fleet between 737-300 and airbus equip. and put the
737-300 in the dca market where it is vulnerable to the noise curfew.
Additionaly all standby crews were eliminated and only 1 spare remained
which was alocated to lga and to be used both for mainline or shuttle
needs. Of note is the fact that the spare has rarely been available.
Most of the time it has been pulled out of base to cover mtc downtimes.
What does all of this say. It says that senior management does not have
it s eye on the operation and we are making to many missteps. Middle
management in some of the operating units is still able to pull off the
same tactics that have worked for years. If senior management continues
to rely on only statistics then they need to be reminded that there are
lies, damn lies, and statistics.
In conclusion let me state that there are at least 2 positives. The first
is that the overwhelming majority of our line employees and extremely
hard working and dedicated to seeing this enterprise survive. Secondly
we are in an improving economy and as we have demonstrated in the past
even the worst managed airline can make money in a good enviroment.
Your comments please
day to day operation.
1. Crew shortage and flight cancellations.
This is not a new problem. It has been an ongoing situation over the
last 13 years...at least. The current shortages have been caused by a
diverse set of circumstances. Some of the problem has been caused by
sick calls...a senior pilot crew scheduler states you can t take 80
pilot sick calls a day and not have a problem. Additional problems
arise when reserve pilot p times..long vs short..are not managed in
a timely manor. Another part of the shortage has been created because
the mtc plan submitted to marketing for each schedule does not come
close to reality causing significant preplanned equipment subs which
depletes both aircraft and crew resources. Yet another part of the shortage
comes from improper planning. You can t schedule crews for a 13 hr 30 min
to 13 hr 59 min duty day operating through phl,lga,bos 3 or 4 times.
The theory that weather was an issue simply is not the case. The weather
only manifests and brings to light the real shortcomings.
2. Mtc planning
In my opinion one of the worst managed areas within the airline. As
stated above the mtc plan submitted to marketing rarely if ever matches
what is required. Heavy mtc requirements do not match nor do the needs
for what are called mtc windows...for the layperson that relates to late
originating aircraft.
We should all remember that summer..not to long ago...when 12 full lines
of 737-300/400 flying were cancelled because mtc got behind on c checks
and had fired the planner who warned senior management that this would
happen. What may not be known is that a team was working on cancelling
3 to 5 lines 757 flying in the days leading up to 9/11. The team was
informed that the f 100 would also be in this position shortly
thereafter. The tragedy on 9/11 effectively cured these problems.
Many of the middle and upper managers that helped to create the
problems are still in charge and similar situations are in the
process of rearing there ugly head. A lie,cheat, and steal attitude
has been prevelant for quite some time and continues unabated.
3. Business travel
Here is a microcosm of what probably are more significant issues. The
operating units were informed that the shuttle made a small profit in
April 2003 and a more significant profit in May 2003 while maintaining
2 spares and weekday standby crews. The marketing response in June 2003
was to split the fleet between 737-300 and airbus equip. and put the
737-300 in the dca market where it is vulnerable to the noise curfew.
Additionaly all standby crews were eliminated and only 1 spare remained
which was alocated to lga and to be used both for mainline or shuttle
needs. Of note is the fact that the spare has rarely been available.
Most of the time it has been pulled out of base to cover mtc downtimes.
What does all of this say. It says that senior management does not have
it s eye on the operation and we are making to many missteps. Middle
management in some of the operating units is still able to pull off the
same tactics that have worked for years. If senior management continues
to rely on only statistics then they need to be reminded that there are
lies, damn lies, and statistics.
In conclusion let me state that there are at least 2 positives. The first
is that the overwhelming majority of our line employees and extremely
hard working and dedicated to seeing this enterprise survive. Secondly
we are in an improving economy and as we have demonstrated in the past
even the worst managed airline can make money in a good enviroment.
Your comments please